Several days of progress:
First was the finished veneer. Even with switching a heatlamp bulb into the drop light, conditions were still a bit off with the veneer. I took to swiping the side of the veneer not getting glue with a cloth dipped in warm water/wringed out. No further issues--just a time consuming cut-test fit-cut-test fit-cut-test fit process, since the frame wasn't a "perfect" hexagon. So much for duplication. I eventually resorted to cutting all my pieces slightly long, and trimming them down from there.
(Side shot, showing trimmed top piece)
(Glued up, rough trim)
(Scraped/relieved)
After finishing the veneering, of the pieces, I fixed the missing ply from the soundboard:
(You'll see in a minute)
I traced the "missing" area on the soundboard using a piece of tissue paper, then duplicated it roughly on a piece of veneer. It's never perfect, so after a few trial and error fits, I scraped it down to see where it was messed up. A combination of using 1) a narrow strip of veneer brought to a point, glued in with hide glue, then pared down to the surface, and 2) the sanded dust from a small piece of veneer, mixed with enough shallac to make a paste (mine was too watery, que será, será), then applied with a card to push it into the deep spots, then sanded down flush--yielded an acceptable repair.
(It'll look even better inside the instrument where you can't see it)
(Coat one of [final tally] fifteen)
I moved on to the end plates, at this point. I new I wanted to bush the key holes...but I didn't want to modify the instrument permanently...which meant that even the thinnest available bushing cloth would be too thick to fit with the existing buttons. I gave it about 5 seconds of thought, and realized that English pianos used leather bushings in some places, so I figured: why not? I skived a piece of leather down to size, trimmed it to width, and pointed it.
(Pull the strip through up to the end, slap on some glue, and stick in a caul)
Long story short...I messed up my math, and the bushings were so thick I couldn't fit the keys in. The glue joint was also too small to ream more than a little of the size...so I threw up my hands, and yanked the bushings out. Oh well...
I moved on to fixing the potential 'leaky' spots on the reed pans using traditional methods: wax. When I had opened up the accordion that I was given, I noted that beeswax had definitely had something added to it, and the color/smell was unmistakable: pine tar. I had already made beeswax/pine tar/turpentine blocks for my waxed canvas stuff, so all I really needed to do was hack a piece off and dilute it with more beeswax. 20 minutes later after baby-sitting the double boiler, I poured it out into the mold, and left it to harden.
(see lower right corner for "missing" glue bead)
(Fixed the other side, too)
You can see the suede of the dampers peeking through the holes above. I wanted to take the time to make sure it was all good (and it was, other than some minor compaction), so I took the action apart.
I used a spring hook tool (indispensable for musical instruments, and oddly enough, mechanical slot machine repair...) to unhook each spring from the lever, before sliding out the pivot rail.
A couple of careful wiggles/tugs later, and I had the levers free.
(Before)
(After carding)
Last stop (today) was cleaning the keys themselves, and replacing all the rubber bands (it's really fuel line hose,
shh) with new pieces, and checking their fit on the action.
After I regulate the other side of the action, I'll be putting it together for a test "firing" to see what needs further attention. I already know that the bellows need a bit of work, but I won't be able to address that until I can actually see/hear where they're leaking...so, soon.
In a few more days, the frames will be ready to rub down with pumice/rotten stone, finishing out the second largest part of the repair.